Can you elaborate a bit more on this as I am not that great with electronics. I am supplying the 5V signal as a DO to the stepper driver via DO1 which is as it is hooked up right now. I just hooked the driver up as they indicated on their drawing. Is there a difference if so how would I fix this?
Would I simply inverse the ground and the power lines within my connections?
Hmmm... My current connections seem to be the same as the LED as I have my nibbles set for the outputs but inversed. 0:3 is my output and 4:7 is my input would this matter? I have my power out to the 5V and as well to the STEP of the driver.
It appears that the issue was with the ramping of the motor itself. There wasn't enough momentum to get the motor spinning at the rpm needed. Do you know of a good way of constantly ramping up the velocity using DAQMX commands until a set frequency?